The
Underwater KP44 Rudder Repair
The clunking rudder, which we had first begun to hear on the passage from
Acapulco to San Christobal, had been weighing on my mind for some time. I had read several stories of KP44 owners
having had rudder problems and one case in particular of a rudder failure at
sea between Fiji and Tahiti.
I didn’t want to risk being at sea with a broken rudder so I looked at
our options. The nearest boatyard and haul out facility where we could get a professional
repair was inEcuador over 600 nm east. I could do the
repairs myself in Puerto Ayora with the help of local workers. We could
continue on our route until we got to someplace where we could haul out and
hope that nothing would break before we got there. I decided that I would do
the work in Puerto Ayora before we left.
At the internet café, I consulted the reports on the Peterson 44 owners’ website written by others who had done rudder work. My plan was to remove the prop, chip away the epoxy over the gudgeons, tie a sling around the rudder, remove the screws and bolts, remove the rudder quadrant, drop the rudder (plugging the hole with a wooden bung), float the rudder away using inflated fenders, and hoist it onto the dinghy using the outboard motor hoist. I’d then take the rudder ashore to cut it open and repair any broken parts inside. That was pretty much how it went although it took quite a long while and six tanks of air to carry out the plan.
It was fortunate that we had a Maxprop feathering prop since this meant that our propeller shaft was a little bit shorter than normal and so we would not have to pull the shaft out to remove the rudder. I would have to remove the prop blades and hub in order to get enough clearance to drop the rudder but I could leave the shaft in place. The rudder is held onto the boat at two points: the rudder shaft goes through the hull at the top of the rudder through a bearing and gland called the rudder packing gland. A mostly watertight seal is created by rings of waxed flax compressed between the bronze rudder post tube and a screw-down collar. The second point of attachment is below the propeller aperture and consists of a gudgeon which clamps over a single pintle. The gudgeon is comprised of two large, flat pieces of bronze that go on either side of the rudder skeg and have flanges at the aft end which meet to form a channel for the pintle. The gudgeon pieces are held together by five very large screws that go through the skeg and a ¾” bolt and nut which compress the pieces together just forward of the pintle. The gudgeons are buried under a layer of fiberglass resin which must be removed.
Happily, we
have dive gear and four air tanks on board Wheatstrong. I spent a couple of
days underwater chipping away the epoxy to expose the gudgeons. The size of the five screws then became
apparent – the heads were a half-inch across with a 1/8th inch slot –
much too large for any screwdriver I had. It took some determined searching to
find a hardware store in Puerto Ayora that stocked a big screwdriver. After paying over $15 dollars for it, I still
had to file the end down to make the bit wider.
Another hour of unscrewing bolts and nuts enabled us to drop the rudder and raise it up onto the dinghy. We took the rudder ashore and loaded it into the back of a truck/taxi and took it over to Jaime. He has a shop at his house and agreed to open up the rudder, do the repairs, fill it, fair it, prime it, and paint it. The cost would be $800 with materials provided by us. We made a Sunday afternoon trip to the Bodega Blanca, a local hardware/marine supply store, where US educated family heir Jason, interrupting his afternoon siesta, opened up the store for us so we could buy epoxy resin, fiberglass mat, and micro-balloons.
It took Jaime and his men a day to cut open a window in one side of the rudder. Inside we found voids, moisture, open cell foam, wood scraps, and a perfectly intact stainless steel internal frame. Whatever the clunking was, it was not due to any internal damage to the rudder. Since we had already torn the rudder open, I took the opportunity to beef it up inside with some additional stainless steel bracing welded into place. We cleaned out all the open cell foam, dried out the inside of the rudder using light bulbs, and filled it with epoxy and micro-balloons. Several layers of glass mat and a lot of fairing and sanding, followed by primer and paint returned the rudder to like-new condition.
The rudder went back onto the boat much easier than it came off. It was just a matter of tying the harness and fenders/floats back on and floating it into position under the rudder post tube then lifting it up using another long line run up through the aft hawse pipes and led to the primary winches. The gudgeons went back on to the pintles as hoped and the rudder packing gland went back on smoothly. The quadrant and steering cables reattached easily on top and, voila, we were back in the steering business. The only problem was that the gudgeons needed to be covered up with epoxy, faired, primed and painted and the Maxprop had to be reassembled. Obviously, the only way to get to the gudgeons for this kind of work would be with the hull out of the water. Additionally, the Maxprop was in about a dozen pieces in a plastic bag on the deck. I couldn't see how I would be able to put that back together by myself underwater. So we began to look for a way to get the boat out of the water - without having to careen her.
At Puerto
Ayora, in the shallow inner harbour there is a drying
rack. To call the inner harbour a harbour at all is a bit
of a misnomer. It would be more accurately described as a shallow, rock bound
cove with barely enough room for dinghies to pass by the half dozen water taxis
and small fishing boats moored across from two tiny dinghy docks. The drying rack is a big concrete frame that
stands on a mud flat; at low tide the rack is completely exposed but at high
tide there is, hopefully, enough water so that you can drive you boat in, tie
up to the rack and then wait for low tide when your boat will be left high and
dry, leaning against the frame. You can
then work on the hull while the tide is out. The only problem is that the inner
harbour is very shallow – too shallow for our six and
half foot draft at all times except for the highest of high tides – which occur
approximately once a month. According to the tide tables we would have enough
water in the inner harbour at high-high tide in a
couple of days to get to the drying rack – with maybe a couple of inches to
spare. We would then have to do the work
and get out before the height of the high tides got too low for us to get out
or risk being stranded on the drying rack for a month until the next high-high
tide. We wrote the necessary letter to
the Port Captain requesting to use the drying rack and, in a day, duly received
permission. We waited a few more days
while a battered old fishing boat overstayed his time on the rack watching the
high water mark gradually decrease until it was finally our turn.
Without a
prop on Wheatstrong we had to tow her to the drying rack through a very narrow,
very shallow channel. I got a local panga driver to help me and I got into our dinghy while
Stephanie stayed on board Wheatstrong.
We pulled up the anchor 30 minutes before the high tide and began to tow
the big boat in towards the narrow entrance to the inner harbour. Things quickly got out of hand as the wind
and current overpowered the little dinghies and their puny outboards. Wheatstrong began to drift towards the rocky
shore and just as the bottom got so shallow so as to allow the keel to touch we
dropped the anchor and racked our brains for a solution to our quandary. It was
now apparent that any attempt to get the boat into the drying rack would be
foolhardy and dangerous so we abandoned that course. The problem now was how to
get the boat out of the coral and rock infested shallows and back into the nice
sandy anchorage. Fortunately, a concerned citizen in a power boat came to our
aid; we threw him a line and he towed us back into the anchorage – after a few
minutes we were back in the anchorage, but not to the same spot we had been in
previously.
The next
day I went underwater to reassemble the Maxprop. I soon discovered that an important piece of
the feathering prop was missing. The
inner hub gear, a bronze piece about the size of my ear, was gone. I had thought the gear was part of the hub
and so had left in place when I took all the other parts off; obviously, it had
been held in place only by the prop’s thick waterproof grease. The turning of the prop-shaft while the
engine ran in neutral at anchor to charge batteries must have caused the inner
hub gear to go spinning off somewhere into the water below. This was a calamity
since there was absolutely no place within thousands of miles that would have
this part. Even having one shipped in
from the US or Italy (where they are made) would take weeks,
if one could even be found. To make
matters worse, the water below us now was not the water that had been below us
before. I had no choice but to go diving at the site where we had been anchored
before we tried to move the boat to the drying rack and look for the part.
I told Steph to go ashore and provision for our departure and took
the dinghy over to the approximate place where we had been anchored. I lined up, as best I could recall, the two
boats we had anchored between and dropped the dinghy’s anchor. Taking a mooring line with me, I went below
and set up a search grid. Using the
line, I searched a 30 foot radius circular pattern around the dinghy anchor. I swam the length of the line and then moved
the line along the arc of the circle six feet then swam it again; and again,
and again, all the way around the circle.
This turned up nothing, so I moved the anchor west 40 feet and searched
again. Still nothing and I was getting
concerned about running low on air. All
the while, dinghies were passing back and forth through the anchorage a few
feet above my head – the whine made by an outboard heard underwater is a scary,
eerie noise. I moved the anchor again
and laid out the grid and began to search.
In desperation I began to stray a few feet further off the line and look
around the sandy bottom for any hint of metal.
I had less than five minutes of air remaining when, out of the corner of
my eye, I saw something that looked like a small rock sticking out of the
bottom. With my heart in my mouth I swam
over and reached down to pull it from the sand.
It was the hub gear. I used up my remaining air whooping and yelping
underwater.
Stephanie
was incredulous when I returned to Wheatstrong with my prize. She hadn’t gone provisioning – convinced that
we would not be going anywhere. I fitted another tank onto my BCD and went back
in to put the prop back together.
Through the liberal use of underwater grease and quite a bit of
perseverance I managed to put the prop back together by myself, underwater. I took the opportunity to adjust the prop
pitch to better match it with the engine and transmission, something I had
wanted to do for quite a while. While I
proved that assembling a feathering prop underwater can be done, I would not
want to do it again and would not recommend it to others. We went in to the store to pick up groceries
and have dinner and a few beers to celebrate the completion of the rudder
repair.